Well I just got finished dynoing.. I hooked the kit back up on Saturday and sprayed 1/2 a bottle through it on sunday and boy did it pull like a mother.. So yesterday I bought a new bottle warmer and today went to dyno.. I dynoed on a Dynojet, the only dyno I trust.. The 1st couple of pulls were on motor and it didnt put down $hit really.. 225rwhp 225 rwtq with a a/f 10.8- 11.0.. I need to get my car tuned with a programer and get my rev limiter raised to 6700.. The maft plus just dont cut it anymore.. That was at 8 percent lean at wot.. The car didnt want to stop pulling at 5600.. Then I warmed up the bottle to 1100 psi.. I still have the 125 shot jets in it.. well the first nitorus pull was really bad.. It hit hard at 3000rpms but right at 4000 it just started to serge.. I only put down 315rwhp and 389rwtq.. I said well that sucks my car on the stock motor put out more power then that.. So I purged and nothing but air.. Then I looked back at my bottles and I forgot to switch them out before we dynoed.. So I strapped in the new full bottle and cut on the warmer.. I got the pressure up to 900 psi and said screw it lets make the pull.. So we ran it and boy does the motor love the nitrous.. It put down 366rwhp and 415 rwtq.. But the best part was that the tq and hp stays up there all the way to rev limiter at 5600 rpm.. It was also only at 900psi... I cant wait to get it up to 1200 psi.. The airfuel was so rich that the dyno didnt even read it from 4000-5600..
So on my stock motor with the 125 shot at 1200 psi I put down 312rwhp and 433rwtq but the tq fell off after 4000 rpms ending at 250 ftlbs at 5600 and 220 hp at 5600.. That was pretty good tune on it too with a a/f 11.8-12.2..
On this motor with the same shot I put down 366 rwhp and 415 rwtq but the tq is over 400 ftlbs from 3000- 5000 and from 5000-5600 its over 350 ftlbs and the Hp doesnt fall off really at all.. This was also at only 900 psi and with a a/f in the low 9's on a stock tune.. I have the video of the good pull and will try to post it tonight when I get off of work..
[ March 09, 2005, 12:55 AM: Message edited by: 1998silverbird ]
So on my stock motor with the 125 shot at 1200 psi I put down 312rwhp and 433rwtq but the tq fell off after 4000 rpms ending at 250 ftlbs at 5600 and 220 hp at 5600.. That was pretty good tune on it too with a a/f 11.8-12.2..
On this motor with the same shot I put down 366 rwhp and 415 rwtq but the tq is over 400 ftlbs from 3000- 5000 and from 5000-5600 its over 350 ftlbs and the Hp doesnt fall off really at all.. This was also at only 900 psi and with a a/f in the low 9's on a stock tune.. I have the video of the good pull and will try to post it tonight when I get off of work..
[ March 09, 2005, 12:55 AM: Message edited by: 1998silverbird ]
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